Posted on Thursday 2 July 2009

After four sets of pistons Craig and I decided to call it quits on the N2O. Not long after we decided to change the combination we found out why it was hurting pistons. A JE piston rep confirmed the pistons were under engineered for the power level. This caused the pistons to collapse over the wrist pins. The fix was to use a heavy small block nitrous piston. We would have really liked to known what this combination would have run after all this time and effort spent on it. In a kind of sad way it was hard to pull all the nitrous off. Not to dwell on the past but look to the future!
A Turbonetics 78mm turbo capable of 1100 hp is in the frame rails. This turbo should give us enough power and reliability for a long time. Well, that is what all the turbo gods have been preaching to us. Well, hell after all this nitrous fiasco I’m game for a new challenge.
Steven



